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Technical Paper

A Rankine Cycle System for Recovering Waste Heat from HD Diesel Engines - WHR System Development

2011-04-12
2011-01-0311
Waste heat recovery (WHR) has been recognized as a promising technology to achieve the fuel economy and green house gas reduction goals for future heavy-duty (HD) truck diesel engines. A Rankine cycle system with ethanol as the working fluid was developed at AVL Powertrain Engineering, Inc. to investigate the fuel economy benefit from recovering waste heat from a 10.8L HD truck diesel engine. Thermodynamic analysis on this WHR system demonstrated that 5% fuel saving could be achievable. The fuel economy benefit can be further improved by optimizing the design of the WHR system components and through better utilization of the available engine waste heat. Although the WHR system was designed for a stand-alone system for the laboratory testing, all the heat exchangers were sized such that their heat transfer areas are equivalent to compact heat exchangers suitable for installation on a HD truck diesel engine.
Technical Paper

A Rankine Cycle System for Recovering Waste Heat from HD Diesel Engines - Experimental Results

2011-04-12
2011-01-1337
A Rankine cycle system with ethanol as the working fluid was developed to investigate the fuel economy benefit of recovering waste heat from a 10.8-liter heavy-duty (HD) truck diesel engine. Recovering rejected heat from a primary engine with a secondary bottoming cycle is a proven concept for improving the overall efficiency of the thermodynamic process. However, the application of waste heat recovery (WHR) technology to the HD diesel engine has proven to be challenging due to cost, complexity, packaging and control during transient operation. This paper discusses the methods and technical innovations required to achieve reliable high performance operation of the WHR system. The control techniques for maintaining optimum energy recovery while protecting the system components and working fluid are described. The experimental results are presented and demonstrate that 3-5% fuel saving is achievable by utilizing this technology.
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