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Technical Paper

Computational Optimization of a Split Injection System with EGR and Boost Pressure/Compression Ratio Variations in a Diesel Engine

2007-04-16
2007-01-0168
A previously developed CFD-based optimization tool is utilized to find optimal engine operating conditions with respect to fuel consumption and emissions. The optimization algorithm employed is based on the steepest descent method where an adaptive cost function is minimized along each line search using an effective backtracking strategy. The adaptive cost function is based on the penalty method, where the penalty coefficient is increased after every line search. The parameter space is normalized and, thus, the optimization occurs over the unit cube in higher-dimensional space. The application of this optimization tool is demonstrated for the Sulzer S20, a central-injection, non-road DI diesel engine. The optimization parameters are the start of injection of the two pulses of a split injection system, the duration of each pulse, the exhaust gas recirculation rate, the boost pressure and the compression ratio.
Technical Paper

Non-Equilibrium Turbulence Considerations for Combustion Processes in the Simulation of DI Diesel Engines

2000-03-06
2000-01-0586
A correction for the turbulence dissipation, based on non-equilibrium turbulence considerations from rapid distortion theory, has been derived and implemented in combination with the RNG k - ε model in a KIVA-based code. This model correction has been tested and compared with the standard RNG k - ε model for the compression and the combustion phase of two heavy duty DI diesel engines. The turbulence behavior in the compression phase shows clear improvements over the standard RNG k - ε model computations. In particular, the macro length scale is consistent with the corresponding time scale and with the turbulent kinetic energy over the entire compression phase. The combustion computations have been performed with the characteristic time combustion model. With this dissipation correction no additional adjustments of the turbulent characteristic time model constant were necessary in order to match experimental cylinder pressures and heat release rates of the two engines.
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