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Technical Paper

Vehicle Driving Cycle Simulation of a Pneumatic Hybrid Bus Based on Experimental Engine Measurements

2010-04-12
2010-01-0825
In the study presented in this paper, a vehicle driving cycle simulation of the pneumatic hybrid has been conducted. The pneumatic hybrid powertrain has been modeled in GT-Power and validated against experimental data. The GT-Power engine model has been linked with a MATLAB/simulink vehicle model. The engine in question is a single-cylinder Scania D12 diesel engine, which has been converted to work as a pneumatic hybrid. The base engine model, provided by Scania, is made in GT-power and it is based on the same engine configuration as the one used in real engine testing. During pneumatic hybrid operation the engine can be used as a 2-stroke compressor for generation of compressed air during vehicle deceleration and during vehicle acceleration the engine can be operated as a 2-stroke air-motor driven by the previously stored pressurized air.
Technical Paper

Vehicle Cooling Systems for Reducing Fuel Consumption and Carbon Dioxide: Literature Survey

2010-05-05
2010-01-1509
The number of vehicles in use is increasing from year to year. It causes more fuel/energy to be consumed, and more carbon dioxide or other exhaust gases are released to the environment. But the legislations on carbon dioxide emissions have become stricter than before. In the overall effort to achieve sustainability, advanced technological solutions have to be developed to reduce fuel consumption and carbon dioxide emissions from vehicles. More than half of the energy in vehicles is lost as heat to the different cooling systems (engine cooling system, air conditioning, frictional components cooling) and exhaust gas. Reducing the amount of energy lost in vehicle cooling systems will enhance the fuel efficiency of the vehicles. This paper presents a literature survey of different cooling systems in vehicles, which includes the engine cooling system, air conditioning of the compartment, the electronic cooling system and cooling of frictionally heated parts.
Technical Paper

Using Oxygenated Gasoline Surrogate Compositions to Map RON and MON

2014-04-01
2014-01-1303
Gasoline fuels are complex mixtures which consist of more than 200 different hydrocarbon species. In order to decrease the chemical and physical complexity, oxygenated surrogate components were used to enhance the fundamental understanding of partially premixed combustion (PPC). The ignition quality of a fuel is measured by octane number. There are two methods to measure the octane number: research octane number (RON) and motor octane number (MON). In this paper, RON and MON were measured for a matrix of n-heptane, isooctane, toluene, and ethanol (TERF) blends spanning a wide range of octane number between 60.6 and 97. First, regression models were created to derive RON and MON for TERF blends. The models were validated using the standard octane test for 17 TERF blends. Second, three different TERF blends with an ignition delay (ID) of 8 degrees for a specific operating condition were determined using a regression model.
Journal Article

Study of the Early Flame Development in a Spark-Ignited Lean Burn Four-Stroke Large Bore Gas Engine by Fuel Tracer PLIF

2014-04-01
2014-01-1330
In this work the pre- to main chamber ignition process is studied in a Wärtsilä 34SG spark-ignited lean burn four-stroke large bore optical engine (bore 340 mm) operating on natural gas. Unburnt and burnt gas regions in planar cross-sections of the combustion chamber are identified by means of planar laser induced fluorescence (PLIF) from acetone seeded to the fuel. The emerging jets from the pre-chamber, the ignition process and early flame propagation are studied. Measurements reveal the presence of a significant temporal delay between the occurrence of a pressure difference across the pre-chamber holes and the appearance of hot burnt/burning gases at the nozzle exit. Variations in the delay affect the combustion timing and duration. The combustion rate in the pre-chamber does not influence the jet propagation speed, although it still has an effect on the overall combustion duration.
Technical Paper

Study of a Heavy Duty Euro5 EGR-Engine Sensitivity to Fuel Change with Emphasis on Combustion and Emission Formation

2010-04-12
2010-01-0872
A diesel engine developed for an international market must be able to run on different fuels considering the diesel fuel qualities and the increasing selection of biofuels in the world. This leads to the question of how different fuels perform relative to a standard diesel fuel when not changing the hardware settings. In this study five fuels (Japanese diesel, MK3, EN590 with 10% RME, EN590 with 30% RME and pure RME) have been compared to a reference diesel fuel (Swedish MK1) when run on three different speeds and three different loads at each speed. The experiments are run on a Scania 13l Euro5 engine with standard settings for Swedish MK1 diesel. In general the differences were not large between the fuels. NO x usually increased compared to MK1 and then soot decreased as would be expected. The combustion efficiency increased with increased RME contents of the fuel but the indicated efficiency was not influenced by RME except for at higher loads.
Journal Article

Some Effects of Fuel Autoignition Quality and Volatility in Premixed Compression Ignition Engines

2010-04-12
2010-01-0607
Previous work has shown that it may be advantageous to use gasoline type fuels with long ignition delays compared to today's diesel fuels in compression ignition engines. In the present work we investigate if high volatility is also needed along with low cetane (high octane) to get more premixed combustion leading to low NO and smoke. A single-cylinder light-duty compression ignition engine is run on four fuels in the diesel boiling range and three fuels in the gasoline boiling range. The lowest cetane diesel boiling range fuel (DCN = 22) also has very high aromatic content (75%vol) but the engine can be run on this to give very low NO (≺ 0.4 g/kWh) and smoke (FSN ≺ 0.1), e.g,. at 4 bar and 10 bar IMEP at 2000 RPM like the gasoline fuels but unlike the diesel fuels with DCNs of 40 and 56. If the combustion phasing and delay are matched for any two fuels at a given operating condition, their emissions behavior is also matched regardless of the differences in volatility and composition.
Journal Article

SI Gas Engine: Evaluation of Engine Performance, Efficiency and Emissions Comparing Producer Gas and Natural Gas

2011-04-12
2011-01-0916
The Technical University of Denmark, DTU, has designed, built and tested a gasifier [1, 8] that is fuelled with wood chips and achieves a 93% conversion efficiency from wood to producer gas. By combining the gasifier with an ICE and an electric generator a co-generative system can be realized that produces electricity and heat. The gasifier uses the waste heat from the engine for drying and pyrolysis of the wood chips while the gas produced is used to fuel the engine. To achieve high efficiency in converting biomass to electricity an engine is needed that is adapted to high efficiency operation using the specific producer gas from the DTU gasifier. So far the majority of gas engines have been designed and optimized for operation on natural gas. The presented work uses a modern and highly efficient truck sized natural gas engine to investigate efficiency, emissions and general performance while operating on producer gas compared to natural gas operation.
Technical Paper

Reducing Throttle Losses Using Variable Geometry Turbine (VGT) in a Heavy-Duty Spark-Ignited Natural Gas Engine

2011-08-30
2011-01-2022
Stoichiometric operation of Spark Ignited (SI) Heavy Duty Natural Gas (HDNG) engines with a three way catalyst results in very low emissions however they suffer from bad gas-exchange efficiency due to use of throttle which results in high throttling losses. Variable Geometry Turbine (VGT) is a good practice to reduce throttling losses in a certain operating region of the engine. VTG technology is extensively used in diesel engines; it is very much ignored in gasoline engines however it is possible and advantageous to be used on HDNG engine due to their relatively low exhaust gas temperature. Exhaust gas temperatures in HDNG engines are low enough (lower than 760 degree Celsius) and tolerable for VGT material. Traditionally HDNG are equipped with a turbocharger with waste-gate but it is easy and simple to replace the by-pass turbocharger with a well-matched VGT.
Technical Paper

Radiocarbon and Hydrocarbon Analysis of PM Sources During WHTC Tests on a Biodiesel-Fueled Engine

2014-04-01
2014-01-1243
PM in diesel exhaust has been given much attention due to its adverse effect on both climate and health. As the PM emission levels are tightened, the portion of particles originating from the lubrication oil is likely to increase. In this study, exhausts from a biodiesel-fueled Euro 5 engine were examined to determine how much of the carbonaceous particles that originated from the fuel and the lubrication oil, respectively. A combination of three methods was used to determine the PM origin: chain length analysis of the hydrocarbons, determination of organic and elemental carbon (OC and EC), and the concentration of 14C found in the exhausts. It was found that the standard method for measuring hydrocarbons in PM on a filter (chain length analysis) only accounted for 63 % of the OC, meaning that it did not account for all non-soot carbon in the exhausts.
Technical Paper

Multi Cylinder Partially Premixed Combustion Performance Using Commercial Light-Duty Engine Hardware

2014-10-13
2014-01-2680
This work investigates the performance potential of an engine running with partially premixed combustion (PPC) using commercial diesel engine hardware. The engine was a 2.01 SAAB (GM) VGT turbocharged diesel engine and three different fuels were run - RON 70 gasoline, RON 95 Gasoline and MK1 diesel. With the standard hardware an operating range for PPC from idle at 1000 rpm up to a peak load of 1000 kPa IMEPnet at 3000 rpm while maintaining a peak pressure rise rate (PPRR) below 7 bar/CAD was possible with either RON 70 gasoline and MK1 diesel. Relaxing the PPRR requirements, a peak load of 1800 kPa was possible, limited by the standard boosting system. With RON 95 gasoline it was not possible to operate the engine below 400 kPa. Low pressure EGR routing was beneficial for efficiency and combined with a split injection strategy using the maximum possible injection pressure of 1450 bar a peak gross indicated efficiency of above 51% was recorded.
Technical Paper

Model Predictive Control of a Combined EGR/SCR HD Diesel Engine

2010-04-12
2010-01-1175
Achieving upcoming HD emissions legislation, Euro VI/EPA 10, is a challenge for all engine manufacturers. A likely solution to meet the NOx limit is to use a combination of EGR and SCR. Combining these two technologies poses new challenges and possibilities when it comes to optimization and calibration. Using a complete system approach, i.e., considering the engine and the aftertreatment system as a single unit, is important in order to achieve good performance. Optimizing the complete system is a tedious task; first there are a large number of variables which affect both emissions and fuel consumption (injection timing, EGR rate, urea dosing, injection pressure, pilot/post injections, for example). Secondly, the chemical reactions in the SCR catalyst are substantially slower than the dynamics of the diesel engine and the rest of the system, making the optimization problem time dependent.
Technical Paper

Mixing in Wall-Jets in a Heavy-Duty Diesel Engine: A LES Study

2014-04-01
2014-01-1127
The paper presents a large eddy simulation investigation on the effect of fuel injection pressure on mixing, in an optical heavy-duty diesel engine. Recent investigation on impinging wall jets at constant-volume and quiescent conditions exhibited augmented air entrainment in wall jets with increasing injection pressure, when compared with a free jet. The increased mixing rates were explained as owing to enhanced turbulence and vortex formation in the jet-tip in the recirculation zone. A recent investigation carried out in an optical heavy-duty diesel engine indicated however a negligible effect of injection pressure on the mixing in the engine environment. The effect of enhanced turbulence and vortex formation of the jet-tip in the recirculation zone is believed weaker than the effect of engine confinement, due to the presence of fuel from adjacent jets limiting the mixing the fuel with the ambient gas.
Journal Article

Lift-Off Length in an Optical Heavy-Duty Diesel Engine: Effects of Swirl and Jet-Jet Interactions

2015-09-06
2015-24-2442
The influence of jet-flow and jet-jet interactions on the lift-off length of diesel jets are investigated in an optically accessible heavy-duty diesel engine. High-speed OH chemiluminescence imaging technique is employed to capture the transient evolution of the lift-off length up to its stabilization. The engine is operated at 1200 rpm and at a constant load of 5 bar IMEP. Decreasing the inter-jet spacing shortens the liftoff length of the jet. A strong interaction is also observed between the bulk in-cylinder gas temperature and the inter-jet spacing. The in-cylinder swirl level only has a limited influence on the final lift-off length position. Increasing the inter-jet spacing is found to reduce the magnitude of the cycle-to-cycle variations of the lift-off length.
Journal Article

Lift-Off Length in an Optical Heavy-Duty Diesel Engine

2015-04-14
2015-01-0793
High-speed OH chemiluminescence imaging is used to measure the lift-off length of diesel sprays in an optical heavy-duty diesel engine of 2 L displacement operated at 1200 rpm and 5 bar IMEP. Stereoscopic images are acquired at two different wavelengths (310 and 330 nm). Subtraction of pairwise images helps reducing the background coming from natural soot incandescence in the OH chemiluminescence images. Intake air temperature (343 to 403 K), motored top dead center density (18 to 22 kg/m3), fuel injection pressure (150 to 250 MPa), intake oxygen concentration (17 to 21 %vol) and nozzle diameter (0.1 and 0.14 mm) are varied and a nonlinear regression model is derived from the experimental results to describe stabilized lift-off length as function of the experimental factors. The lift-off length follows the general trends that are known from spray vessel investigations, but the strength of the dependence on certain variables deviates strongly from those studies.
Technical Paper

Investigation and Comparison of Residual Gas Enhanced HCCI using Trapping (NVO HCCI) or Rebreathing of Residual Gases

2011-08-30
2011-01-1772
A comparison between throttled and unthrottled spark ignition combustion with residual enhanced HCCI combustion is made. Early intake valve closing and late intake valve closing valve strategies for unthrottled spark ignition combustion are evaluated and compared. Approximately 3-6 percent relative improvement in net indicated efficiency is seen when comparing unthrottled spark ignition combustion with throttled spark ignition combustion depending on valve strategy and engine speed. The relative improvement in efficiency from spark ignition combustion to HCCI combustion is approximately 20 percent for the conditions presented in this study. The rebreathing strategies have the highest efficiency of the cases in this study.
Technical Paper

Investigation and Comparison of Multi Cylinder Partially Premixed Combustion Characteristics for Diesel and Gasoline Fuels

2011-08-30
2011-01-1811
Partially Premixed Combustion is a concept able to combine low smoke and NOx emissions with high combustion controllability and efficiency. It is of interest to be able to utilize PPC in a large operating region in order to meet the Euro VI emission legislation without relying on NOx aftertreatment. This paper investigates the differences in PPC characteristics for three fuels; Diesel Swedish Mk 1, Low Octane Gasoline (70 Octane) and US Standard Gasoline (87 Octane). Engine operating conditions, combustion characteristics, emissions and efficiency are in focus. The experiments were carried out at a range of operating points on a Volvo MD13 which is a six-cylinder heavy-duty engine. At each operating point three combinations of EGR level and λ-value were evaluated. 1. High EGR/High λ, 2. High EGR/Reduced λ, and 3. Reduced EGR/High λ.
Technical Paper

Investigating Mode Switch from SI to HCCI using Early Intake Valve Closing and Negative Valve Overlap

2011-08-30
2011-01-1775
This study investigates mode switching from spark ignited operation with early intake valve closing to residual gas enhanced HCCI using negative valve overlap on a port-fuel injected light-duty diesel engine. A mode switch is demonstrated at 3.5 bar IMEPnet and 1500 rpm. Valve timings and fuel amount have to be selected carefully prior to the mode switch. During mode transition, IMEPnet deviates by up to 0.5 bar from the set point. The time required to return to the set point as well as the transient behavior of the engine load varies depending on which control structure that is used. Both a model-based controller and a PI control approach were implemented and evaluated in experiments. The controllers were active in HCCI mode. The model-based controller achieved a smoother transition and while using it, the transition could be accomplished within three engine cycles.
Technical Paper

Influence of Inlet Pressure, EGR, Combustion Phasing, Speed and Pilot Ratio on High Load Gasoline Partially Premixed Combustion

2010-05-05
2010-01-1471
The current research focuses in understanding how inlet pressure, EGR, combustion phasing, engine speed and pilot main ratio are affecting the main parameters of the combustion (e.g. efficiency, NOx, soot, maximum pressure rise rate) in the novel concept of injecting high octane number fuels in partially premixed combustion. The influence of the above mentioned parameters was studied by performing detailed sweeps at 32 bar fuel MEP (c.a. 16-18 bar gross IMEP); three different kinds of gasoline were tested (RON: 99, 89 and 69). The experiments were ran in a single cylinder heavy duty engine; Scania D12. At the end of these sweeps the optimized settings were computed in order to understand how to achieve high efficiency, low emissions and acceptable maximum pressure rise rate.
Technical Paper

Impact of Mechanical Deformation due to Pressure, Mass, and Thermal Forces on the In-Cylinder Volume Trace in Optical Engines of Bowditch Design

2011-01-19
2011-26-0082
A detailed investigation is made of the impact of mechanical deformation on the in-cylinder volume as function of crank angle degree in an optical engine of Bowditch design. The squish height is found to change linearly with mass and pressure forces. It increases due to pressure forces and decreases due to mass forces. The thermal forces have an impact on the squish height but it is not clear in what direction. The volume change caused by deformations did not change the calculated load significantly but gave errors during heat release calculations. Two different strategies to reduce these errors are presented.
Journal Article

Ignition Quality Effects on Lift-Off Stabilization of Synthetic Fuels

2015-04-14
2015-01-0792
The ignition and flame stabilization characteristics of two synthetic fuels, having significantly different cetane numbers, are investigated in a constant volume combustion vessel over a range of ambient conditions representative of a compression ignition engine operating at variable loads. The synthetic fuel with a cetane number of 63 (S-1) is characterized by ignition delays that are only moderately longer than n-dodecane (cetane number of 87) over a range of ambient conditions. By comparison, the synthetic fuel with a cetane number of 17 (S-2) requires temperatures approximately 300 K higher to achieve the same ignition delays. The much different ignition characteristics and operating temperature range present a scenario where the lift-off stabilization may be substantially different.
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