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Technical Paper

Effects of Nozzle Hole Diameter and Injection Pressure on Flame Lift-Off and Soot Formation in D.I. Diesel Combustion

2011-08-30
2011-01-1813
Previous research has shown that the reduced nozzle hole diameter and elevated injection pressure are effective for preparing a uniform fuel-air mixture in a direct injection (D.I.) Diesel engine. A micro-hole nozzle with a hole diameter of 0.08 mm and an ultra-high injection pressure of 300 MPa have been employed to investigate the mixture formation process under various conditions. The aim of the current work is to clarify the effect of nozzle hole diameter and injection pressure on flame lift-off and soot formation processes. The free sprays from the micro-hole and conventional nozzles were investigated at a high-temperature, high-pressure constant volume vessel. A high-speed video camera system was employed to record the non-vaporizing sprays and combustion. The direct photography of OH chemiluminescence was used to provide information about the high temperature combustion process and to measure the flame lift-off length.
Technical Paper

Split Injection Spray Development, Mixture Formation, and Combustion Processes in a Diesel Engine Piston Cavity: Rig Test and Real Engine Results

2018-09-10
2018-01-1698
The objectives of this study are to investigate the effects of premixed charge compression ignition (PCCI) strategies with split injection on soot emission characteristics. The split injection conditions included three injection intervals (1.1 ms, 1.3 ms, and 1.5 ms) and three injection quantity fraction ratios (Q1/Q2 = 10.0/14.6 mm3/st, 15.2/9.4 mm3/st, and 20.0/4.6 mm3/st). The results in real engine tests showed that shorter injection intervals, and the 1st injection quantity contributes to reduced soot emissions. A rig test with high-pressure and high-temperature constant-volume vessel (CVV) and a two-dimensional (2D) model piston cavity were used to determine correlations between injection conditions and soot emissions. During the rig test, fuel was injected into the CVV by a single-hole nozzle under split injection strategies. The injection strategies include the same injection intervals and quantity fraction ratios as in the real engine test.
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