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Technical Paper

Balancing Design Functional Coupling and Sensitivity to Noise to Achieve the Design Target

2007-04-16
2007-01-1207
The primary objective in design is to achieve the target value of the design's response function. If a design fails to achieve the target value, it most likely fails in two ways: inconsistent functional output and in design involving multiple response functions, unable to converge to the multiple target values in spite of iterative adjustment of the design parameters. The former is symptom of a design not able to perform in the presence of variability, i.e., noise. The latter is symptom of a design that fails to perform in the presence of functional coupling. Both problems are best addressed at the conceptual stage of the design at which only design solution that is inherently robust to noise and functionally uncoupled is entertained. If this is not possible, the alternative is to exploit the interaction between control variables and variables that are sources of noise and functional coupling to render the design insensitive to them.
Technical Paper

Gear Whine Reduction for a New Automatic Transmission

2001-04-30
2001-01-1506
Gear whine in 1st and 2nd gears in a new rear wheel drive automatic transmission was identified as a potential customer dis-satisfier. Improvements to the vehicle system were implemented, but did not sufficiently reduce the noise. CAE modeling and hardware testing were used for gear tooth optimization, transmission system, driveline, and vehicle system studies. The planetary gears were re-designed with increased contact ratio, and significant interior noise reduction was achieved; but some vehicles still had excessive noise due to gear parameter variability from multiple sources. Using a DOE and statistical studies, a set of gear parameter targets were identified within the tolerances of the design, which achieved the program objectives for noise.
Technical Paper

The Anatomy of Knock

2016-04-05
2016-01-0704
The combustion process after auto-ignition is investigated. Depending on the non-uniformity of the end gas, auto-ignition could initiate a flame, produce pressure waves that excite the engine structure (acoustic knock), or result in detonation (normal or developing). For the “acoustic knock” mode, a knock intensity (KI) is defined as the pressure oscillation amplitude. The KI values over different cycles under a fixed operating condition are observed to have a log-normal distribution. When the operating condition is changed (over different values of λ, EGR, and spark timing), the mean (μ) of log (KI/GIMEP) decreases linearly with the correlation-based ignition delay calculated using the knock-point end gas condition of the mean cycle. The standard deviation σ of log(KI/GIMEP) is approximately a constant, at 0.63. The values of μ and σ thus allow a statistical description of knock from the deterministic calculation of the ignition delay using the mean cycle properties
Technical Paper

Vibration Measurement in Flight

1937-01-01
370175
EQUIPMENT for measuring vibration in airplane structures and powerplants during actual flight is described in this paper. This development is the result of a cooperative research program carried out by the Bureau of Aeronautics of the U. S. Navy and the Massachusetts Institute of Technology with contributions of improvements in design and new features by the Sperry Gyroscope Co., Inc. In its essentials, the M.I.T.-Sperry Apparatus consists of a number of electrical pickup units which operate a central amplifying and recording unit. The recorder is a double-element photographic oscillograph. Each pickup is adapted especially to the type of vibration that it is intended to measure and is made so small that it does not appreciably affect the vibration characteristics of the member to which it is attached rigidly. By using a number of systematically placed pickups, all the necessary vibration information on an airplane can be recorded during a few short flights.
Technical Paper

Seat System Key Life Test

2000-03-06
2000-01-1190
An accelerated seat durability test was developed to identify potential problems in areas with traditionally high warranty cost and customer dissatisfaction: squeak & rattle and mechanism looseness & efforts. The test inputs include temperature, humidity, road vibration, occupant movements, and mechanism cycling. These inputs were combined into a single 14-day test profile that simulates 10 years and 250,000 km. (approximately 150,000 miles) of 95th percentile customer usage. Various components of the seat assembly are tested together as a system. The test was performed on two current production programs. The test produced issues similar to those found in warranty repair data and evaluations of used seats from high-mileage customer-owned vehicles.
Technical Paper

A Comparison of Different Squeak & Rattle Test Methods for Large Modules and Subsystems

1999-03-01
1999-01-0693
Many engineers today use large, powerful multi-purpose test systems to do squeak & rattle testing of modules and subsystems such as Instrument Panels, Consoles and Seat Assemblies. Such test systems include Multi-Axis Hydraulic Shaker Tables and Electrodynamic Vibration Systems with large head expanders and rigid (or at least stiff) fixtures. These test systems have been successful when used for squeak & rattle test programs, have been validated as approved test methods, and have become the standards of comparison in many labs today. They are, however, expensive and throughput can be limited due to the time needed to unbolt, unload, handle, load, and re-bolt a test item at its many attachment points on the rigid fixture. Furthermore, the capital cost of these Legacy systems can be prohibitive, especially for the smaller supplier, who is being compelled to perform squeak & rattle testing on the products they supply to their customers, the vehicle manufacturers and Tier 1 suppliers.
Technical Paper

Use of Binaural Measurement and Analysis Techniques in the Establishment of Steering Pump Design Tolerances for Noise, Vibration and Harshness Performance

1999-05-17
1999-01-1852
The objective of the present work was to establish a correlation between steering pump cam ring profile location and steering system performance for noise, vibration and harshness (NVH). Once this correlation was established, the secondary objective was to determine acceptable cam profile position tolerances from the standpoint of NVH performance. These objectives were accomplished through the use of binaural measurement and jury evaluation of vehicle interior noise. Cam rings were manufactured for this study with profiles shifted a predetermined distance away from the nominal position. These cams were built into steering pumps and these pumps were in turn installed in a vehicle. Vehicle interior noise and pump housing vibration measurements were made to quantify the steering system noise performance associated with each cam ring. The interior noise recordings were played back for a jury comprised of engineers familiar with steering system noise.
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