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Technical Paper

A Study of the Rankine Cycle Generating System for Heavy Duty HV Trucks

2014-04-01
2014-01-0678
In heavy duty (HD) trucks cruising on expressway, about 60% of input fuel energy is wasted as losses. So it is important to recover them to improve fuel economy of them. As a waste heat recovery system, a Rankine cycle generating system was selected. And this paper mainly reports it. In this study, engine coolant was determined as main heat source, which collected energies of an engine cooling, an EGR gas and an exhaust gas, for collecting stable energy as much as possible. And the exergy of heat source was raised by increase coolant temperature to 105 deg C. As for improving the system efficiency, saturation temperature difference was expanded by improving performance of heat exchanger and by using high pressure turbine. And a recuperator which exchanges heat in working fluid between expander outlet and evaporator inlet was installed to recover the heat of working fluid at turbine generator. Then a working fluid pump was improved to reduce power consumption of the system.
Technical Paper

Evaluation of Low Phosphorus Engine Oil Containing MoDTC

2007-07-23
2007-01-1962
Phosphorus levels in engine oil are assumed to be lower than other oils because they cause emission catalyst poisoning. It mainly originates from zinc dithiophosphate (ZnDTP), which is an essential additive for engine oils as an antiwear agent and antioxidant. The reduction of ZnDTP in engine oils will have a great influence on this. On the other hand, fuel efficiency in vehicles is also an important issue and molybdenum dithiocarbamate (MoDTC) is very effective in improving fuel economy. Oils containing MoDTC with phosphorus content from 0.00% to 0.08% were tested using several engine and bench tests to evaluate their antiwear properties, oxidation stability and friction reduction durability. In these tests, oils containing more than 0.02% of phosphorus were able to fulfill ILSAC GF-4 performance standards with optimized additive formulation. MoDTC helped to replace several functions of ZnDTP in low phosphorus engine oils.
Technical Paper

Experimental Study for High Specific Load Bearings in the Diesel Engine

2002-03-04
2002-01-0297
Recently, exhaust emission has been enforced on diesel engines for the countermeasure of environmental problems. Accordingly, the cylinder pressure in the engine is being increased to improve fuel efficiency, the engine bearings must be used under severe conditions of high specific load. Because the connecting rod bearings, particularly of diesel engines, are used at high specific loads that exceed 100 MPa, elastic deformation of the bearing surface occurs, and the oil film thickness decreases at the edges of the bearing length in the axial direction. This causes the bearings to contact with the crankshaft, thus resulting in the wear of the bearings, which could even result in seizure. The following factors contribute to seizure: bearing materials, bearing shapes, machining methods, and incorrect assembly. Focusing on these factors, this study evaluated the behaviors exhibited by connecting rod bearings in actual engines by using the rig testers.
Technical Paper

Mechanism of and Fuel Efficiency Improvement by Dimple Texturing on Liner Surface for Reduction of Friction between Piston Rings and Cylinder Bore

2014-04-01
2014-01-1661
Reducing friction between the piston ring and cylinder is an effective way of meeting the demand for lower fuel consumption in vehicle engines. To that effect, the authors have proposed a new and efficient friction reduction treatment for the cylinder. At first glance, this treatment seems similar to typical microtexture treatments, but it is built on a different approach. Through a rig tester, it was confirmed that optimizing the shape of the dimples and the treatment area for the cylinder improves FMEP between the piston ring and the cylinder liner by 17%. This report presents an analysis of the test results to explain the mechanism by which this effect is achieved. Fuel consumption was measured in an actual engine, and a maximum fuel consumption improvement of 3.2% was confirmed after conversion to the Japanese heavy duty vehicle fuel economy standards (Category T2). Lubricating oil consumption, blow-by and durability were also examined.
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