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Technical Paper

Pump Noise Reduction Using Shainin Statistical Engineering Methods

2001-04-30
2001-01-1542
Historically, pump noise can be a contributor to customer dissatisfaction with automatic transmissions. In this paper, a Shainin experiment was conducted to identify all probable root causes for pump noise on a production RWD transmission. Sample transmissions were selected following subjective evaluations. Noise was objectively measured in the lab using a microphone and an accelerometer. The study was conducted following a systematic Shainin statistical engineering methodology, which included the following major steps: selection of the test measure using the isoplot technique, selection of Best of Best (BOB) and Worst of Worst (WOW) transmissions, assessment of assembly variation, component search, and pair-wise comparisons. The study successfully highlighted the key variables on the drive gear involute profile, which are now being tightly controlled for improved noise characteristics.
Technical Paper

Methodology for Vehicle Box Component Durability Test Development

2004-03-08
2004-01-1690
During the initial vehicle design phase and as the first prototypes are built, extensive on-board instrumentation and data acquisition is required at the proving grounds (PG). The data is used for various types of testing and analysis. During this phase of development very few parts and assembly components are available for physical test. The objective is to develop a component test for the truck box. This test can be run without suspension parts during the early stages of the vehicle development. A further objective is to correlate the test to FEA models and actual Proving Ground full vehicle test results.
Technical Paper

Design and Development of the DaimlerChrysler 5.7L HEMI® Engine Multi-Displacement Cylinder Deactivation System

2004-05-07
2004-01-2106
Cylinder deactivation is a means of improving the fuel economy of gasoline engines. This paper covers the application of the technology to a V8 engine and implementation into vehicles. The description of the engine hardware and its operation are discussed. The engine and transmission control strategy are described, including an example of the compensation strategies to smooth the transition between the different modes of engine operation. The powertrain and chassis hardware changes required to address the noise vibration and harshness issues are discussed and examples of untuned systems are shown.
Technical Paper

Torque Converter CFD Engineering Part II: Performance Improvement through Core Leakage Flow and Cavitation Control

2002-03-04
2002-01-0884
The performance of a large-volume production torque converter is slightly different from those of development prototype due to the core leakage flow. The sealing gap between the stator crown and pump or turbine core of the production converter is usually larger than that of prototypes because of fabrication method and tolerances. In this work, the core leakage flow of torque converter was investigated using CFD. The core region was modeled and coupled together with other three major components of a converter. Studies show that for a particular converter the core leakage flow could result in a 3.6% stall torque ratio reduction and a 2% peak efficiency decrease. The effects of sealing gap dimensions were also studied. Computational investigations in this work indicated that the variation of input K factor with input torque level observed in dyno tests is due to the cavitation in the torque converter.
Technical Paper

Torque Converter CFD Engineering Part I: Torque Ratio and K Factor Improvement Through Stator Modifications

2002-03-04
2002-01-0883
To improve vehicle launch feeling, the powertrain torque output needs to be largely increased. Compared with modifications to engine, transmission, and axle, one of the most inexpensive ways of achieving this goal is to modify the torque converter to get a higher stall torque ratio. In other applications, in order to lower engine speed for better fuel economy, and to match with a higher output engine, a converter with higher torque capacity (lower K factor) is also often desired. In some case of small-volume production, the torque converter modifications are limited to the stator only in order to reduce the manufacturing cost. In the present study, the engineering CFD simulations were used to develop new stators for stall torque ratio and K factor improvement. The flow fields of both baseline and modified torque converters were simulated. The overall performances of the converter were calculated from the flow field data, and correlated with the dyno test data.
Technical Paper

Drivetrain Torsional and Bending Vibration for a RWD Vehicle Interior Noise Development

2003-05-05
2003-01-1496
In a vehicle NVH development and refinement phase, it is necessary to understand the source of the noise and vibration from various powertrain and drivetrain mechanisms. The noise and vibration generated by a drivetrain in a vehicle is a complicate but significant source of physical mechanism, which might become important issues in early or later phase of the vehicle development. For the diagnostic purpose of the drivetrain, a rear-wheel drive (RWD) vehicle in early development phase has been used to measure the bending and torsional vibration of the drivetrain, as well as the vehicle interior noise simultaneously, while the vehicle is running up and down under quasi-steady state on a chassis dynamometer. The lower frequency resonances of torsional and bending vibrations from the drivetrain are correlated with the vehicle interior boom or overall loudness.
Technical Paper

Proactive Ergonomic Verification Through Human Biodynamic Modeling and Digital Simulation

1999-09-28
1999-01-3371
An extensive digital simulation study on lift devices that interact with human operators in DaimlerChrysler automotive assembly plants has been initiated and deployed. This digital mock-up of human-machine workcells is to scientifically evaluate and further certify a number of typical commercial lift devices that are served in car-assembly operations. The entire model is based on human biomechanical Jacobian relationship, as a fundamental kinematic structure, to predict human body instantaneous joint-torque distribution when the human is working with a certain payload. The developed modeling and simulation system will play a pivotal role in proactive ergonomic prediction, verification and digital certification in car advance manufacturing engineering processes.
Technical Paper

Achieving Acceptable Cp and Cpk Values in Sheetmetal Stampings

1999-09-28
1999-01-3193
Detail parts are approved during several different phases of the prototype build cycle. There is much pressure at all stages to meet strategic body quality targets. Parts stamped for assembly must meet a process capability requirement of Cpk>1.33. For final PSO (process sign off), as called out in the PPAP (Production Part Approval Process) manual, the requirement can be increased to meeting a Cpk>1.67. During the 2000 Neon part approval process, the PPAP requirements provided the guideline necessary for consistent buy-offs. However, on some critical parts the Cpk requirement made part approvals difficult to accomplish. Occasionally this caused resources to be focused in the wrong place. This paper will discuss how a requirement of Cpk>1.33 can make part approvals more difficult to achieve and change the entire application of a tolerance.
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